Since we last
updated, Team Yolette has been hard at work injection molding and
reworking our molds in order to finally manufacture plastic parts for
our yo-yo! In this blog entry, we highlight the challenges we have
faced and overcome in manufacturing the red and black insert part
discussed in the last blog entry.
On our first run of
injection molding the “color ring,” we found the correct lengths
of ejector pins & shim by finding the difference between the size
of the mold and the given dimension of the whole ejector pin &
mold assembly, and then loaded our molds into the injection molding
machine. Using a set of starting process parameters similar to
previous parts, we injection molded our first parts, hopeful, but not
expecting that it would work on the first attempt. After adjusting
the screw feed stroke such that plastic was filling over the whole
profile and the mold was filled as much as possible, we found that
our part was not being filled entirely.
First try at color ring |
In order to remedy this, we
decided to machine additional runners that looped around to the edge
of the part opposite the sprue so that it would fill better.
We milled out two additional runners on the cavity side, and tried
again. However, this time we found that because of the large size of
the new runners, the part was getting stuck in the cavity after
molding, and was therefore not ejecting (we should probably have put
these runners on the core). In order to remedy this, we went back to
the mill and added ejector pins on the runners, which we then
threaded in order to help the core side ‘grip’ the part, keeping
it on the correct side (core) until ejection. This new mold worked
well, and the only remaining defects we observed were that there was
some dishing in the rectangular pieces, which we found to be
acceptable since it does not have any mating and is nearly invisible,
and that the mold stuck a tiny bit in the core side, but this was not
a problem as it still ejected consistently. We used a very short
cooling time in order to allow the part to shrink more, as the
shrinkage was initially smaller than we predicted (2%). We were
therefore able to use a short screw feed delay time, allowing for
rapid production.Color ring cavity |
Color ring core |
Final process parameters |
Next time on our
blog: completed yo-yos!!
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